Replies: 6 comments 4 replies
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Do the logs (typically /var/log/syslog) report any errors? Do the time and distance keep going? What happens when you set naturalDeceleration to 0 (this selects a different stroke detection algorithm)? |
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Yes, checking the logs is a good idea. Especially check if the impulses from your rowing machine are still recorded when your stroke count stops. |
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@laberning The syslog says Aug 13 19:20:44 OpenRowingMonitor npm[606]: *** Calculated drag factor: 29311.31 After that, the strokes are counted only very irregularly. However, the number of meters increases. |
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Just a wild guess, the Calculated drag factors in your logs varies quite a bit. Eventhough you are not using these because you have set Set the engine log level to debug in your config and have a look if something goes off the rails with the stroke detection (maybe the noise filter settings need some adjustments): // Available log levels: trace, debug, info, warn, error, silent
loglevel: {
// The default log level
default: 'info',
// The log level of of the rowing engine (stroke detection and physics model)
RowingEngine: 'debug'
}, You can use these commands on the command line to restart and retrieve the logs after changing the config: restart after config changes: Get the status of a service: Show the log output of a service: |
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It is a bit better with autoAdjustDragFactor: false but even here it does not count some strokes |
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Please, Set maximumTimeBetweenImpulses to 1.0 and naturalDeceleration to 0. I've written the RowingEngine, I have tuned three rowers to work ORM, I know what I am talking about. |
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Hello,
I have the problem that for some reason the counting of the beats stops after ~2 minutes.
I use a customized version of the WRX700 profile for this Rowing Machine https://www.ebay.de/itm/234569647424?var=534203620753
VENDOMNIA: {
numOfImpulsesPerRevolution: 1,
autoAdjustDragFactor: false,
naturalDeceleration: -5.0,
flywheelInertia: 0.72,
dragFactor: 32000
},
Anyone have any idea what the problem could be?
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