We have recently encountered a situation where the board's response to throttle input is unresponsive, with voltage readings remaining stagnant at an oscillation between 0 and 1 volts even when full throttle is applied. After thorough analysis, it has become apparent that there might be a slight discrepancy in the current scaling and voltage synchronization with our motor of choice or there might be an issue with the calibration of the board and motor. It would be helpful if you could suggest a few measures to overcome the issue.